Despite all the hoopla, mechanically the consumer version 1984 Fiero Indy Pace Car is essentially still the fully-optioned white 2M4 SE it started out as. All SE's have the WS6 performance suspension and quick ratio steering rack.
The Indy Package (RPO Y82) added a new Aero-nose fascia, ground effects, new rear fascia and wing with interior and exterior cosmetic packages. There were a couple cosmetic touches on its stock 4-cylinder 92hp "Iron Duke" engine and dual exhaust added. Other than a choice of automatic or manual transmission, all the Indy models that were produced were identical and performed the same as any other 20-second 1/4 mile "Iron Duke" Fiero.
Indy #163 came to me (I'm 3rd owner) with a 3.3L SD4 engine and TH125 automatic.
Just the start of "after" pics. Starting to look good now.
Once the engine was out and in the shop, the first order of business was getting some basic mechanicals cleaned up.
The front bodywork had already been pulled off to examine the how extensive some prior accident damage had been. After cleanup/touchup of everything, it was reassembled.
Here's the cleaned/painted front suspension parts. Although I replaced the worn steering rack bushing and tie-rod ends, once the car was driveable, it steered terribly and adjustment of the pinion pre-load was never able to correct the inherent looseness. I ultimately replaced the entire rack with another one from Pick 'n Pull.
Here's the front suspension reassembled. I scrapped the original rusted rotors, and used "like new" rotors I removed from my GT when I did the Lebaron rotor brake upgrade. New SS brake lines, calipers and Porterfield R4-S pads make up the new braking system. I later installed a new master cylinder when it became apparent the old one was no good.
The ball joints were replaced - MOOG "problem solvers" on the upper, and Dickman's 1" lowering balljoints on the lower. Monroe shocks were installed on the front. Energy suspension poly bushings were used for the sway bar and 4" long endlinks. I also decided to install the front springs that came off my GT (thinner wire). The suspension actually moved now.
Part numbers Energy Suspension PN 9-5158 - black poly sway bar bushings for 7/8" bar w/brackets Energy Suspension PN 9-8118 - 4" endlinks with black poly Monroe front shocks PN 5921 Moog upper (problem solver) ball joints PN K5292
At the rear, the balljoints seemed OK and left in place. After cleanup and painting of the control arms, Prothane poly bushings were installed. New Monroe struts and Eibach rear springs were purchased for installation when the cradle would be reinstalled.
I had an '86 cradle that I cleaned up and painted for the new engine and transmission. The control arms were installed and the Addco rear sway bar was fitted.
As for the braking system, new SS brake lines, calipers and Porterfield R4-S pads were also installed on the rear. In addition, all 3 parking brake cables were replaced.
Part numbers Monroe rear struts PN 71814 Prothane control-arm bushings PN 7-304 Addco sway bar (rear) PN 387
[This message has been edited by fierosound (edited 11-06-2008).]
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01:26 PM
KurtAKX Member
Posts: 4008 From: West Bloomfield, MI Registered: Feb 2002
All this talk on the Indy Fiero raises questions as to why GM didn't make the SD4 available as an option. The original Indy cars were SD4's but GM ended up offering only a cosmetic copy with a Duke engine for the entire production run. I believe that the answer is that the move was political. An Indy Fiero with an SD4 would have outperformed the Corvettes of that era. GM top brass probably couldn't live with a sports car selling at 1/2 the cost with the ability to blow away a Corvette.
------------------ 87GT - 3800SC Series III engine, 3.4" Pulley, N* TB, LS1 MAF, Flotech Exhaust Autolite 104's Custom CAI 4T65eHD w. custom axles, HP Tuners VCM Suite. 87GT - 3.4L Turbocharged engine, modified TH125H " I'M ON THE LOOSE WITHOUT THE JUICE "
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01:53 PM
PFF
System Bot
Bremertonfiero Member
Posts: 390 From: Bremerton WA USA Registered: Sep 2008
Since the engine needed rebuilding (in spite of assurances that it didn't), I decided to replace the stock TH125 3-speed automatic (3.18 final drive) with a stronger 4T60 4-speed automatic with a 3.33 final drive (35/35 gears). I purchased a new rebuilt from one of the most reputable shops in town.
This non-electronic transmission uses both a TV (Throttle Valve) cable AND vacuum modulator to control shifting. The TV cable is synchronized with the thottle to control shift points, downshifting etc. while the vacuum modulator (get adjustable one) controls line pressure and the firmness of the shifts.
The ECM controls the Torque Convertor Lockup (TCC). To do this the ECM uses input from the MAP, TPS, VSS and engine TEMP sensor. To retain ECM control of the TCC these sensors would need to be retained and a TPS needed to be mounted to the intake manifold. There's other standalone alternatives for TCC control as well.
At a later time, once the car was up and running, I didn't like the 3.33 final drive (35/35 gears), so I dropped the cradle again to have the transmission gearing changed to a 3.73 final drive (33/37 gears) which was much better match with the engine performance and the larger 15" wheels I would be using. Runs 70mph at about 2400rpm with 215/60R15 tires.
Stock transmission and engine mounts were used at first. It later became apparent that this tilted the engine/tranmission toward the trunk firewall and would cause manifold clearance issues. The first indicator that something was off was that the axles didn't seem to line up correctly. Hadn't anyone ever noticed this before?
It became more apparent when we test fit the engine. I was not possible to get the 4-cylinder intake on because there wasn't enough clearance between the head and firewall. Basically, the front of the transmission was too high and the mount needed to be modified. Before and after pictures.
The bracket sits on the end of the intake manifold and the 3/8" thick plywood is a mockup of this thickness.
Changing the front transmission mount brings everything back in line. The intake manifold will now fit.
The rubber was burned off the stock Fiero bracket. An Anchor Industries 2266 mount (67-69 Dodge Dart 273 V8 engine mount) is used. It is about 1-inch thick and has 2 offset mounting bolts. It was positioned and a bolt was drilled in the Fiero bracket. It was then bolted in place between the transmission side bracket and the Fiero bracket. The assembly lines up with the second set of bolt holes in the cradle. This positions the transmission correctly.
Both the right and left axle assemblies for a 1989 Pontiac 6000 (with 2.8 V6, 4T60 and light duty brakes w/o ABS) were purchased. There are plenty of other combinations of parts that can be used to assemble DIY axles that will fit, but this was the simplest solution. These have the correct mating ends for the transmission and the 20mm diameter spindle to match the Fiero hubs. They can be purchased off the shelf at most auto parts stores and install directly without modification.
Part numbers A1 CARDONE PN 601078 - LEFT side drive axle (21-inches long overall) A1 CARDONE PN 601115 - RIGHT side drive axle (26.25-inches long overall)
A Derale transmission cooler was installed to handle transmission cooling requirements. The radiator didn't leak in static testing, so it was reinstalled. Later it turned out that coolant would seep out around the edges of the driver's side end tank once the system was hot and pressurized. A new radiator was installed at that time.
[This message has been edited by fierosound (edited 11-06-2008).]
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08:45 AM
Nov 10th, 2008
fierosound Member
Posts: 15190 From: Calgary, Canada Registered: Nov 1999
Not much interest in any of this?? Someone paints their car yellow and there's 5 pages of comments?
Here's what I did on the interior. It was completely removed and a thorough cleaning of the door panels and all other components was undertaken. The floor mats and carpeting was steam cleaned. The sun-faded "blue" speaker grills were recovered with new speaker fabric. The shifter surround and shifter plate were reglued.
While the interior was out, sound proofing was installed as well as a new stereo system.
To still maintain a "factory" look a Pontiac CD player was installed, but high-end equipment was used in all hidden locations. New Clearwater speakers were installed in the seat headrests and Infinity component speakers went in the dash.
A factory sub-woofer housing with a Tang-band sub went into the factory location.
To power the sub, a Xtant 1.1i 100 watt mono amp was used. This tiny amp really delivers and is perfect for the job because it can be installed under the passenger seat.
When I received the car, the radio surround was terribly warped and needed to repaired or replaced.
The lack of an oil pressure gauge in the instrument cluster REALLY bothered me because I consider that the MOST important gauge to have. That's why I installed GT gauges and a new radio surround. It's "factory", looks correct, does the job and I needed to replace the warped radio surround anyway. I still have a 2nd voltmeter in the tach, but that's not a big bother.
I never did like the original T-bar type automatic shifter and most others eithers are either too big (Cobra head type) or look wrong (aftermarket aluminum). I found something perfect from 84-96 Corvette - a small size, top-button, dark grey leather wrapped knob that suits the car's interior perfectly. This is smaller than a similar design used in other GMs like Cavaliers, Grand AMs etc. I mounted it on a shortened shifter shaft and installed a new leather boot I purchased from Rodney Dickman.
The previous owner sold the original "mint" Indy seats. Although the Mr Mike's leathers were nice, I'd have preferred a set of originals, but another set of mint seats are few and far between. As luck would have it, we found some OEM red embossed Indy seat fabric which I purchased and had sent off to Mr Mike. Mike did up a beautiful set of repro Indy seats.
I cleaned up the rusty seat rails and repainted them and bought the proper light grey color recliner covers to replace the incorrect dark grey ones the seats in the Indy came with. Once assembled, only an Indy purist would notice that these are not the original seats. The only difference is that the backs of the seats aren't grey fabric like the originals.
The terrible condition of the sunvisors and headliner required that they be replaced. I bought new sunvisors and a headliner recover kit from the Fiero Store. It was a bit of work, but I successfully recovered and reinstalled the headliner and the new visors. I also added the coathooks - 84's didn't have any.
More to come. The engine is next...
Edit: pictures added
[This message has been edited by fierosound (edited 01-28-2009).]
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09:53 AM
87_special Member
Posts: 266 From: San Diego, CA Registered: Oct 2006
Thank you. Here's a shot of the front compartment. After getting the damage to the hood repaired, the underside was repainted. The overflow and windshield washer tanks had both yellowed, so I replaced them with new ones from Fiero Store. I had the spare tire cover from some time ago and decided to use it here.
[This message has been edited by fierosound (edited 11-10-2008).]
Both the right and left axle assemblies for a 1989 Pontiac 6000 (with 2.8 V6, 4T60 and light duty brakes w/o ABS) were purchased. There are plenty of other combinations of parts that can be used to assemble DIY axles that will fit, but this was the simplest solution. These have the correct mating ends for the transmission and the 20mm diameter spindle to match the Fiero hubs. They can be purchased off the shelf at most auto parts stores and install directly without modification.
Part numbers A1 CARDONE PN 601078 - LEFT side drive axle (21-inches long overall) A1 CARDONE PN 601115 - RIGHT side drive axle (26.25-inches long overall)
That's great Info on the transmission, I was given one that I would like to use in one of my cars, pending on its driving condition.
[This message has been edited by FieroWannaBe (edited 11-10-2008).]
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01:56 PM
wftb Member
Posts: 3692 From: kincardine,ontario,canada Registered: Jun 2005
Wow Tony! All I can say is that sure isn't the car I delivered to you way back when. Though I don't pretend to have any special insight into the car, I did transport it and therefore was under the car to tie it down and did a pretty close inspection to note any issues prior to transporting it. It was a pretty nice but typical car with the exception of the SD4 in the engine bay and a pretty nice interior. You've really transformed that ride into something special. Congrats
Ron
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04:59 PM
fierosound Member
Posts: 15190 From: Calgary, Canada Registered: Nov 1999
I saw this car a few years back at Carlisle when the previous owner showed it and it looked nothing like you have it looking now. For the money that you paid it should have looked like this when you received it. Not trying to rub it in but just wanted to complement your fine work. Do the future plans include converting to EFI? The Webers that you have are efficient carbs but there is no room for any real air filtering. I believe that EFI would boost cold weather starting, efficiency, drivability and gas mileage With a 4BBL manifold from Clifford you could bolt on a Holley TB or even an AC Delco injection system.
------------------ 87GT - 3800SC Series III engine, 3.4" Pulley, N* TB, LS1 MAF, Flotech Exhaust Autolite 104's Custom CAI 4T65eHD w. custom axles, HP Tuners VCM Suite. 87GT - 3.4L Turbocharged engine, modified TH125H " I'M ON THE LOOSE WITHOUT THE JUICE "
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06:31 PM
The_Stickman2 Member
Posts: 1030 From: Lehigh Valley Pa. Registered: Sep 2007
Actually an intake from Clifford research won't work on a Super Duty head. It will bolt up alright. But the ports on the SD-4 head are so big they are actually taller than the intake flange in those intakes. Same with the stock ones. Not sure about the Holley TBI intake.
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07:02 PM
Dennis LaGrua Member
Posts: 15477 From: Hillsborough, NJ U.S.A. Registered: May 2000
Actually an intake from Clifford research won't work on a Super Duty head. It will bolt up alright. But the ports on the SD-4 head are so big they are actually taller than the intake flange in those intakes. Same with the stock ones. Not sure about the Holley TBI intake.
Well, it looks like the four expert has me proved wrong again but what do you expect from a diehard V6 man? Then I must acknowledge that the SD4 head ports must be huge, so much so, that even porting the Clifford intake won't do it. The Holley TB FI system will bolt up to any manifold that is drilled for a Holley carburetor but since we don't have such a manifold then that takes out that option unless an intake can be made up from mandrel tubing with a flange welded to it or we modifiy an SD4 manifold. A while ago I read the performance specs of the SD4 and geeze that engine screams!
------------------ 87GT - 3800SC Series III engine, 3.4" Pulley, N* TB, LS1 MAF, Flotech Exhaust Autolite 104's Custom CAI 4T65eHD w. custom axles, HP Tuners VCM Suite. 87GT - 3.4L Turbocharged engine, modified TH125H " I'M ON THE LOOSE WITHOUT THE JUICE "
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10:00 PM
Raydar Member
Posts: 40925 From: Carrollton GA. Out in the... country. Registered: Oct 1999
...I didn't like the 3.33 final drive (35/35 gears), so I dropped the cradle again to have the transmission gearing changed to a 3.73 final drive (33/37 gears) which was much better match with the engine performance and the larger 15" wheels I would be using.
Before I did my 5 speed swap, I was also contemplating doing this with a 4T60, to use with my 3.4. Did you do the work yourself? Do you know how difficult it was?
------------------ Raydar 88 4.9 Formula IMSA Fasback..........................88 3.4 coupe -soon to be something other than red
Wow Tony! All I can say is that sure isn't the car I delivered to you way back when. Though I don't pretend to have any special insight into the car, I did transport it and therefore was under the car to tie it down and did a pretty close inspection to note any issues prior to transporting it. It was a pretty nice but typical car with the exception of the SD4 in the engine bay and a pretty nice interior...
IDo the future plans include converting to EFI? The Webers that you have are efficient carbs but there is no room for any real air filtering. I believe that EFI would boost cold weather starting, efficiency, drivability and gas mileage With a 4BBL manifold from Clifford you could bolt on a Holley TB or even an AC Delco injection system.
Nope. We don't have the expertise up here to get something like that tuned and working properly. If it was a Chev or Ford V8 - no problem. Everybody's an "expert" in those things to the point where they don't have to think. And THAT's the problem. It's like the problem I had when I went Supercharged - it's outside everyone's area of expertise. The engine shop never saw a 4-banger like this before - luckliy all they needed was a complete copy of the SD4 guide.
Keep in mind, this will not be a daily driver, won't be driven in winter weather at all and will be primarily a summer weekend driver and a Show and Shine participant.
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07:46 PM
Lilchief Member
Posts: 1738 From: Vevay,Indiana Registered: Feb 2004
Fierosound: Very impressive rebuild. Just a few questions. How does the SD 3.3L compare to the 2.8 or even a 3.4 ? Or is it closer to a SC 3.8 ? Have you ran any 1/4 mile times? And what kind of gas mileage does it get? You said something in the lines of engine work, what are your plans? Do you have any specs on the present engine,hp, tq, internal components? Just curious cause I'm working on a 3.0L SD/Merc for my 88 coupe. Well a big 2 thumbs up on your project. I like it.
------------------
85 GT 3.4 14.9 @ 90 1.9 60' Old TH125/3.06 Unknown New 4T60/3.42
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08:06 PM
PFF
System Bot
Nov 13th, 2008
fierosound Member
Posts: 15190 From: Calgary, Canada Registered: Nov 1999
The real "meat" of the project was the 3.3L SD4 engine.
After all, that was the BIG selling point "Dirty Rat" Chester was bragging about and supposedly made this Indy such a bargain for whoever "bought in" to what he was saying. https://www.fiero.nl/forum/A...070315-4-032634.html
Unfortunately, contrary to everything that was said, the engine did need a complete rebuild and many $$$.
The cylinders had some wear and we determined that the pistons had .008" piston-to-wall clearance - way too much!! That explained in part the low compression test readings of 92psi. JE pistons specify a .0045" piston-to-wall clearance for their pistons (these were JE's).
The engine block went through all the usual rebuild procedures. The block was hot-tanked, align honed, decked, cylinders bored and honed for 4.020" diameter pistons, and new freeze plugs installed.
The new Stainless Steel intake valves are 2.055" diameter and the exhaust valves are 1.600" in diameter. Here's a comparison of what came out and the new SS valves that would be installed.
The bare head was cleaned up, milled, and new bronze guides installed, along with the new SS valves, dual valve springs, keepers and locks. According to the SD4 engine guide, the Paul Vanderley designed SD4 heads out of the box (before any porting) flow 88% more than a stock Duke head!
The installed billet Crane roller camshaft was designed for solid roller lifters and a 1.55 ratio. It had been sent to Geoff at Colt Cams Inc (Langley, B.C.) and was reground to a suitable single-pattern hydraulic roller street/strip profile compatible with the new CR of 10.5, and the Crane Gold 1.7 ratio roller rockers that were on the engine.
Operating RPM range of the cam with matching springs is 2000-6500rpm. New hydraulic roller lifters and hardened pushrods will complete the valvetrain. A steel camshaft gear set was used to drive the camshaft off the crank.
I had the crank and rods magnafluxed to make sure they were OK. They passed inspection and were then prepped for the engine. The crank bearing surfaces were ground/polished and the connecting rods had their ends resized.
The head cc'd at 58cc in the combustion chambers. It was calculated that a 4.020" zero deck piston with a 20cc dish would give us a 10.5 to 1 compression ratio - should be workable with premium pump gas.
Here's the "goods" waiting to go into the readied block after coming back from balancing - pistons, reground crank, and resized rods.
...and a couple of shots of the reassembled short block.
You can see some minor grinding in the block walls required to clear the connecting rod throws.
Once they had the head installed, I would be bringing it home!
I've got a quick question. Do you have other projects you're working on at the same time, or are you JUST focusing all your attention and time to this one vehicle? Only reason I ask is because the attention to detail is amazing... I've done work of that quality as well, but now that I'm stupidly juggling 3 projects, I find that I just don't have the time to sand down every part and repaint it.
Also, that sound deadening material, is that dynomat type stuff? I typically install stuff like that in cars that I fix up, but I'm hesitant to do it on my 87 Fiero since I don't want to line the floorpans with stuff I won't be able to remove. Is the stuffy tacky, or does it just lay in there?
...but now that I'm stupidly juggling 3 projects, I find that I just don't have the time to sand down every part and repaint it.
Is the stuffy tacky, or does it just lay in there?
Thanks everyone, been working on it since Sept 2006. You'll find that working on more than one project at the same time means none ever get finished.
The soundproofing I used is a peel & stick roofing material that seems to made of a similar material to Dynamat. Thought I’d try it. Covered it here in the stereo thread: https://www.fiero.nl/forum/Forum2/HTML/081643.html
The “other car” - 87 GT - is kinda done. Just maintaining it so it keeps winning awards. It's been jealous of the attention on the Indy.
------------------
3.4L S/C 87 GT www.fierosound.com 2002/2003/2004 World of Wheels Winner & Multiple IASCA Stereo Award Winner
[This message has been edited by fierosound (edited 11-14-2008).]
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03:49 PM
Nov 15th, 2008
fierosound Member
Posts: 15190 From: Calgary, Canada Registered: Nov 1999
I saw this car a few years back at Carlisle when the previous owner showed it and it looked nothing like you have it looking now. For the money that you paid it should have looked like this when you received it. Not trying to rub it in but just wanted to complement your fine work.
I'd have to agree with you. What really shocked me was how "beat up" the car was for something with ONLY 19,000 miles...
I've seen cars with 50,000 miles or more that still look BRAND NEW so I don't think I was out of line expecting this to be better than it was.
[This message has been edited by fierosound (edited 11-17-2008).]
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12:01 PM
Nov 17th, 2008
fierosound Member
Posts: 15190 From: Calgary, Canada Registered: Nov 1999
Wo-hoo!! The assembled long-block engine is painted and on the cradle.
Here it is with the timing cover, harmonic balancer and water pump installed. My machine shop matched the old ruined harmonic balancer with one from a Chevy truck 6-cylinder engine. All that was required was slight boring to fit the crank and cutting of a new timing mark.
We did a test fit of the cradle and that's when we confirmed that something was not sitting right with the way the engine/transmission was mounted. We had "pushed" the engine to get the dogbone bolted up, but the Edelbrock 4-bbl manifold did not fit between the head and trunk firewall. There was LOTS of head scratching trying to figure this one out.
Only after checking things over and over again, we discovered that mounting the transmission on stock Fiero mounts tilted the powertrain back, because the front transmission mount is too high and needed modification. I'd never seen this mentioned anywhere before, but then the V6 engines aren't as close to the trunk firewall so people likely haven't noticed.
When I bought this car, Chester said it "only needed" a custom mounting block for a hi-torque starter because nobody made one to fit the SD4. Actually, Tilton has a high-torque starter to fit the SD4 and has it listed on their website. I had it in my hands before the car arrived!! But it was immediately obvious that it needed more than a new starter, battery, oil change, coolant and fresh fuel to get this thing running.
I then found a Tilton starter with a butchered mounting block that they'd been trying to fit, in the Indy's trunk! The problem wasn't lack of a suitable starter, but the way the solenoid is "clocked" when the Tilton starter is installed. The starter only fits this way because the offset gearing doesn't permit clocking it to get the solenoid on top - the motor hits the block. The solenoid clashes with the header's primary pipe from cylinder #4 because of the way the it is tilted outward.
Rather than try to modify the way the starter mounted to the engine (as Chester had tried), it was necessary to change the header - either to a different one, or modify the one we have. Finding new headers of any type for the Fiero Duke was impossible, so I decided to modify the old header.
You can see that the while header's primary pipe from cylinder #4 would clear the stock starter with solenoid directly on top, it would now clash with the Tilton starter's solenoid.
The "Competition" Hooker header was a 4-into1 long primary tube design. It wasn't especially suited to the street because of the way it ran under the cradle and reduced road clearance - a liability if the car is lowered. You also can't install a rear sway bar because of it.
I decided on a compromise and modify it into a 4-into1 "shorty" design header. We cut back the tubes to change the location of the collector, and changed the routing of the primary pipe from cylinder #4 to clear the starter. After modification and the final welding, the entire header was ceramic coated.
A ceramic coated exhaust heat shield was also installed. It shields the water pump and A/C compressor from exhaust heat at the front of the engine, and protects the wiring and starter to some degree on the transmission end. The 3" exhaust runs under the cradle and just clears the rear sway bar below it.
On the other side of the engine I installed an Paul Vanderley designed Edelbrock Victor Jr 4-bbl aluminum manifold. The SD4 head had already been ported, so both the intake gasket and intake manifold were ported to match the head. Prior to installation, the manifold was clear powder coated to protect it and keep it looking good. It is topped with a polished Edelbrock AVS 4-bbl carburetor.
An ATI polished aluminum carb bonnet will be directing air into the carburetor. This item is originally intended for use in supercharged or turbocharged blow-through carburetor applications. As it happens, it matches the new polished Edelbrock valve cover topping the engine perfectly.
The ONLY valve cover gasket you want to use on the Duke is Felpro PN FEL-VS50179T - especially with this Edelbrock valve cover. Don't use the cork or cork/rubber ones as they always tend to leak. This rubber/steel gasket has raised edges to seal properly and comes with all the hardware needed for installation.
The distributor I decided to use was a coil-in-cap HEI design with centrifugal and adjustable vacuum advance as this would be the best and simplest solution and because of the great number of performance items available. I'm using an MSD distributor module and MSD coil with it.
The distributor's centrifugal advance was tailored to bring in 38* by 2800rpm and limited to 52* total with vacuum advance. Magnecor plug wires send the charge to Autolite spark plugs. DEI boots protect the plugs and boots from the heat of the headers.
At the front of the engine, it was now possible to use the proper dogbone/alternator bracket and dogbone. The clunky old alternator was tossed in favor of the newer smaller CS design used on the 88 Fieros. Braided lines drain oil from connections on the intake manifold to inlet ports in the Miloden oil pan.
A new exhaust was built, header to tips. I used a Flowtech Afterburner cross-flow muffler designed for the Camaro. The dolly is pushing up on the exhaust pipe which is why it looks like the muffler is hanging crooked in this picture.
In the meantime, I also got the engine bay ready. The old ratty insulation was removed, everything scrubbed down and paint touched up as needed, before new OEM looking insulation went in.
[This message has been edited by fierosound (edited 11-18-2008).]
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08:36 AM
The_Stickman2 Member
Posts: 1030 From: Lehigh Valley Pa. Registered: Sep 2007