Small update while I'm here.
I forgot my camera last time I was down. To bad too. It was a very productive weekend.
I finally got the car out for some real test drives. Everything went pretty smooth. It drove better then I expected. The speedo is not working though. Actually I'm not sure if Aaron did the conversion to my chip to directly run the speedo or not. I'm going to try adding one of Rockcrawls conversion circuits (I bought it almost a year ago) and see if I can get that working. As a last resort I will go with VSS to PCM to Speedo connected in series. Hopefully the circuit will work.
The car drove so well on the test drives I decided to start puting it back together. I later installed most of the rest of the interior pieces. The new seats went in also... Damn, they look good!
New locks were installed for the deck and doors, center skeleton was put back in the car, heater controls and rear view mirror were robbed from parts car, PCV vent was added, purge canister wired in and vaccume lines re-arranged back to factory specs per the service manual. I also discovered that it was not a belt chirp I was hearing. Come to find out the alternator has a bad bearing in it. Course that was after I had already re-made the tentioner bracket. The altenator/starter rebuilders up the street say they have a replacement bearing for me so I won't have to replace the whole alternator. I will give me a chance to rebuild it fully anyway. I know there are many other things I got done but I can't think of them right now.
After finishing up all this stuff it was time to pack up for the trip home. I got everything put away and decided to move the car outside. It now idles very well and felt better then it ever had before. I was very suprised how much of a difference the purge canister made all by itself. Really smoothed out the idle.
Of course, now the car has developed a new problem. I seems to be because the RPM's drop so fast when letting off the gas. The PCM can't compensate fast enough and the car dies. If I ease off the gas it in not a problem. I think I was just taking it easy on the first couple drives so it never got a chance to do it. I'm going to try grounding C10 and F7 now and see if that doesn't solve the problem as per MickeyMoose suggestion in the "building a 4.9 swap harness" thread (pg 4).
I will also be doing the tach modification and will dial it in with a scanner. I'll post a small write up on how to do this when I get it working. I broke down and bought the scanner since I need to pull the codes and check sensor readouts. Now I'm in kind of a hurry and have to get this car going. My daily driver is dying fast.
I will still be working to get the BCM, ECC, and FDC working in the car but things are not going very smooth for this right now. I can't get the displays to light. They need 16v and my understanding is that came from the BCM. Once I get it figured out we will have the ability to do an idle/tps learn to dial everything in further aswell as all the other things you can do with this system. I'll keep you all posted.
Oh, one more thing. My headlights do not come up. I believe the isolation relay is bad in this car. I think there is an extra on the parts car... hopefully. This car needs to be on the road by 6-2 so that I can take it up to Arlington on 6-7. I think I might just make it.
[This message has been edited by Fieroseverywhere (edited 05-24-2008).]